I’ve spoken to Watermill Carriage Co today as I’m heading down there at the end of the week to have a look at the car prior to picking it up. There are a few more things to report in terms of the work carried out to the car.
The reason the windscreen was loose was because the sealing rubber was missing. However, on fitting the replacement seal it appeared the old screen wouldn’t fit with the new rubber in place. It turns out the screen was 8mm thick rather than the correct 6mm. This has meant fitting a new screen. I must make a mental note to order a Triplex sticker for the windscreen.
In addition to the boot carpet a new cover panel kit has been fitted to the boot to hide the fuel tank.
The door handles were indeed upside down so these have been corrected which is a relief as I looked at hundreds of photos and wondered if I was going mad.
I have at last found the decals I bought for the air cleaners (which have now been painted and fitted) so I can take these down with me. In addition, I also found the brass manifold nuts I bought at great expense (well, it seemed expensive for a few nuts anyway). These should dress the manifold a bit and they are the correct type rather than the steel ones currently fitted.
I’ve also ordered a new 48 spoke 4J spoked wheel for the spare wheel compartment which will be fitted with a 155/15 tyre so it fits properly. Along with this, I’ve also ordered some new double eared knock on/off spinners to replace the current ones that have seen better days. I’ve also ordered the leather strap kit for the spare wheel compartment for the wheel and tool kit. I need to order a jack now and find somewhere to store the hide and copper mallet I’ve bought.
The engine is running now apparently and news is it sounds very sweet. The erratic idle has been resolved (an air leak). There are a couple of small causes for concern that need resolving.
- The overdrive isn’t engaging properly even though the solenoid is activating. Thoughts are that this is an alignment issue and “should” be simple to cure. On the basis nothing has been simple on this car I’m not holding out any hope of a simple fix.
- The starter motor is being troublesome and is not throwing 100% of the time. If can’t easily be fixed I’ve suggested to Watermill that they source an original type as the one fitted is a high torque type and they don’t sound great although they are a common upgrade.
So the plan is to head down to Watermill on Friday to have a look over the car and make sure any loose ends are tied up, then get the car MOT’d and collect it next week somehow. I’m still in two minds whether to try to drive it back (with all the issues of getting to Cornwall without driving somehow) or wait a further week and get it collected.